Monday, December 30, 2013

Phase 1 of Phase I

Now that I am back in the flying business again, I started on completing Flight 1 of the Production Acceptance Procedure (PAP) which is the very phase 1 of Phase I. I tried to do a mix of maneuvers from the PAP and keep the fun part up by flying the plane a bit for sight-seeing and playing with the SkyView to get more comfortable with the avionics.

Basic stalls out of slow flight, straight and  level and with slight bank angle have all been completed during the 3rd flight that verified that the pump was working ok. Then I also checked the 120 knots behavior in an extended dive from the exercise altitude of 4500 AGL.

Today I completed the 4th flight of N128TL and the most demanding yet. I took about an hour of flying time trying to stall the plane from a 10-15 degree bank angle. It is almost impossible to do that as the plane resists to get the nose up at lower speeds and the pressure on the elevator becomes very hard to overcome. You have to be very heavy handed to get into a stall on a turn at 60 knots.
I also tried to squeeze the left flaperon trailing edge to reduce or eliminate the heavy right wing. So far I made little progress on the heavy wing but my hands were pretty tired after two runs along the trailing edge.

Here are some pictures from the airstrips around my home airport.




I also covered the oil cooler just a tad to get the oil temps up to boiling water level. This amount works great in 10C ambient temperature.


Now that I am done with Flight 1, I am having a problem to continue as the next flights require me to run the engine at the maximum continuous RPM of 5500 and my tachometer is still misbehaving at around 5000. I have no clue at this point what it could be and don't know what to do about it. I'll see if the forum can help ...

Update: The forum helped but even more so did Mel, a friend of Gary who also finishes an RV-12 at Marana. Mel suggested to increase the inline resistance of the RPM signal path from the 30K Ohms Van's had put in to an overall 50K Ohms. I will try to add the additional 20K Ohms on Saturday and test the result.

Saturday, December 28, 2013

She's Flying Again

After closing everything up yesterday and doing a successful engine ground run with some time at WOT with pleasing fuel pressure and flow indications, I did a 50 minutes test flight today.
I can say it feels good to be flying again and the fuel supply did not show any issues whatsoever.
The only problem that is left is the erratic RPM readings once I reach 5100 RPM. Obviously my attempted fix in securing the plug that connects the avionics to the cable coming from the Rotax did not solve the problem. I will have to dig into that at some point but don't see the need for it right now.
Currently I am more hampered by the small test flight area of just 25nm around my home airport. At 110 knots you reach the edge of the area pretty quickly! The following pictures shows the North North-West edge of that area.


and the Skyview at the same location, showing 117 knots TAS at 4900 feet and at only 5070 RPM. This plane is really fast, and I haven't even installed the wheel and leg fairings yet!


Now I have to read into the flight testing exercises and get to it!

Thursday, December 26, 2013

It Was The Pump, And The Pump Alone!

Today I put the new fuel pump in and hooked it back up to the lines. I didn't tie it down all the way and used clecos to hold the shelf down for a first trial run.


I filled another gallon of gas into the tank, opened the valve and flipped the switch. Whoosh! A strong stream of gas was rushing into the canister underneath the gascolator. What a beautiful sight! No hesitation, no fuzz, just pure gas and a lot of it.

The 1-gallon drain test was done in around 120 seconds. It ended so abruptly that I had a hard time finding the stop button on the watch (or the cell phone for that matter).

I checked the pump fittings and found no leaks and finalized the pump installation, riveting the shelf back to the belly skin and reconnected the pushrods to the torque tubes.


Then I closed up the panels in the baggage area and put the seats back in.


What is left is to close up the belly access panels and then reinstall the cowls. A ground test run will follow and then ... maybe some flying!

Wednesday, December 25, 2013

Bad Fuel Pump

So I got an early Christmas gift a few days ago when I was out at the hangar again. The task was to determine a bit further if the fuel pump had an issue or not. I had made some flared tube stubs that would allow me to hook up tubes to the pump while it was in the fuselage and pump some gas in a closed circle - just to see how the pump rate was.
Before I attached these stubs, I decided to remove the inlet fitting after fishing in there with a tiny hook and finding some small pieces of unidentifiable debris.


What I found was traces of rust on the inside of the fitting. I grabbed my inspection camera and got a photo of the inlet side of the pump.

The shots taken from the screen of the camera are a bit blurry but I think you can still see the problem clearly enough,



Where did the rust come from? Well, I thought of the best way a while back to pressure test the fuel system before putting gas in it. Back then I decided to use distilled water which I tried to vacate after the test using pressurized air. Obviously this was not enough to get it out or maybe it just wasn't a good idea to put it in there to begin with. Either way, the pump had to come out.

Before doing that (which I deemed a multiple days job) I wanted to see if the pump really was the problem for limiting the flow in the fuel system and so I hooked up the tube stubs (after tightening the fitting again) and attached some PVC hoses to pump gas around in a jerry can.
Well, the result was inconclusive. The pump does slightly restrict the flow when blowing into it from the intake side but not enough to cause such a restricted flow as I had seen when doing the last-gallon test. When pumping real gas, it did do a pretty decent job in my eyes. It showed much more flow than I had seen during the last-gallon test. But then, I had also messed with the system since then quite significantly, so maybe the problem had disappeared or at least was mitigated at this point? I also do not remember seeing any problems during the First Flight and I did pretty much the same long and steep climb out at WOT as I did on the second flight when I saw the flow/pressure problem.
While the pump definitely has to be replaced because of the obvious rust problem, it is not yet clear to me that the pump was the only cause for the problem I had seen. There still could be something wrong with the tank as well.
For now I had to take the fuel pump out though and that was something I had not looked forward to at all. Before ripping everything apart I wanted to give it a serious try to remove it without further unscrewing of bulkheads and seat pans and such.

I drilled out the 4 rivets on the belly to get the shelf loose to which the pump is screwed on to. This was necessary as the pushrods prevent a direct access to the AN4 bolts that hold the pump to shelf and I did not have any tools to work around the rods. With shelf loose I could move sideways just enough to get a socket to them to remove them. With the pump disconnected from any mechanical restraints, it was fairly easy to detach the electrical connection as well. The pushrods were detached at their aft connection point to the torque tubes so I was able to spread them easily and with the pump being moved aft I was able to get it out by turbing it 90 degress while pulling it up and away from the tunnel. The distance from the flange on the bottom to the intake and outlet fittings is just enough to clear the pushrods with a 90 degree turn and then it was free.



One additional problem I have seen once the shelf had come out is that I had primed the flange area between the shelf bottom where it touches the belly skin. The flange has to make electrical contact for the ground of the pump though and at this point it could only do that through the 4 rivets that were holding it to the skin. I do not think that was a very good connection and it might have limited the current for the pump as well. I removed the primer with MEK and will not reprime it but maybe put some conductive grease on it when putting it back in.
The new pump is at home in the shop and will be readied with fittings and electrical connector to be a drop-in replacement for the rusty one.

The fact that the pump came out so "easily" will make the further work so much nicer and was a great Christmas gift! Now I can put the replacement pump in and test it much quicker than I had anticipated. I might still have an additional flow problem but at least I did not have to remove the seat pan, bulkhead and the flaperon servo just to get the pump out.

Merry Christmas!

Monday, December 16, 2013

More On The Fuel Flow ...

I have finally overcome my paralysis and went back to the hangar to take the fuel system apart in my hunt for the bug that causes gas to just drizzle slowly out of the gascolator (when the bowl is removed).


By disconnecting the pushrods for the flaperons in the back where they are attached to the control horns, I was able to push them outboards just enough to allow a wrench to unscrew the nuts on the fuel pump fittings.



Once the lines were unhooked from the pump I was using a PVC hose to attach to the lines and blow some air through it (careful with the line between tank and pump! Remove the cap before doing this so to not inflate the tank). Both lines were free of any noticeable restrictions. The forward line was a little less open but I could hear the hissing, turbine-like sound of the flow transducer as the air was rushing through, so I am sure I got great flow.

I want to order some more fittings to confirm that it is indeed the pump that is causing the slow flow and not the tank before I go about removing the pump. Also, I want to be able to confirm that the replacement pump is indeed working better than what I have in the fuselage right now.

Thursday, December 5, 2013

It Wasn't In The Gascolator...

So I spent another night at the hangar trying to determine what is causing my fuel pressure issues. I opened the gascolator and found, practically nothing. The screen is clean and nothing indicated that it wasn't clean all along. What to do?
I decided to drain the rest of fuel out that I couldn't get with my handy ATV pump which amounted to about 5 gallons. I turned on the electric pump and put a bucket under the gascolator to catch the gas. This turned out to be an almost hour long ordeal as the flow was that minimal. The Skyview showed a flow of 6.4 gallons per hour and the amount drained and the time needed verified that it was pretty accurate.
I felt compelled to do the drain test for the last gallon which is part of the PAP and instead of 181 seconds (which would have been sufficient) it took me almost 20 minutes to squeeze that gallon out of the tank.
This clearly indicates a problem between the tank and the gascolator. When the flow started to be somewhat slow at the beginning of the drain, I removed the fuel cap to see if it was a venting issue but that did not have seemed to make a difference on the flow rate.
The next tests will be to remove the fuel line at the electric pump and to see which side has the restriction. My hopes are that the fuel pump is the culprit as this would be easier to fix than an issue in the tank or in the fuel lines (maybe the lines wouldn't be so problematic but I doubt accessibility would be easy).

To be continued...

Tuesday, December 3, 2013

Cowls Removed

With my recent experience of always underestimating the time to remove stuff from the airplane, I decided to drop by the hangar after work and get started on my fuel supply problem by removing the cowls.
That took indeed the better part of the little daylight that is left at the end of the workday now. I even got to remove the safety wiring from the gascolator screws, which turned out to be harder than putting the wire on those screws (!).
I also pumped out most of the leftover gas from the tank using a Facet ATV electric fuel pump system to reduce the amount I will have to wash through the open gascolator. Did I mention that I really hate sloshing around fuel in open containers?
I got the screws out and left the bowl in its place as it was getting really dark at that point and the lighting in my hangar is more on a level for emergency lighting than for working through the night.
Before I left I also inspected the carb spillover pans and found traces of a few drops of gas that had washed away some dust there. As I had a few high fuel pressure warnings through the first flight I wonder if this was the result of that or if dirt got into the carb bowls and breached the valve that should have prevented the bowl from overfilling. I will certainly have to run a test with the cowl removed when the fuel system is put together again.

Sunday, December 1, 2013

Second Flight, First Problem

Before I start on the second flight, let me tell you that there won't be a video from my first flight. The GoPro had worked fine but when I tried to read out the video, my Mac froze up and the mounted NTFS file system of the SD card got damaged upon the reboot. It was beyond repair and so I had to format the card. Fortunately, I was able to take a video (with much better landings) on my second flight which will get posted here when I had time to put it all together.

On the second flight I did a touch&go before leaving the pattern for a long climb out to 6000 feet. At around 4500 feet I noticed that the engine seemed to slightly lose thrust. Because of the still erratic RPM gauge I could not tell if this was indeed true. Scanning the engine monitor showed that I had a fuel pressure of just 0.7 psi which would explain why the Rotax did not develop its full power. I decided to throttle back after verifying that I had the electric fuel pump working. As soon as I throttled back a bit the pressure started rising again. A sure sign of a clogged fuel system.
I did some speed tests up to 112 knots which showed that I do not need a rudder trim tab as she was flying straight as an arrow when I took my feet off the pedals.
After another 30 minutes of flying time I did another touch&go and a full stop landing, heading back to the hangar. I will remove the cowls and open the gascolator bowl to clean out whatever might be in there that restricts the fuel flow. I might have to also to the flow test from the tank , through the pump to the gascolator to see if that part is clean. I just hope I don't have to pull the carb bowls as this means some additional parts removal to just get to them.

Thursday, November 28, 2013

Successful First Flight

The morning was still breezy so I decided to stay at home and watch the wind forecasts. It said it should die down at noon (how unusual).

We went out there to arrive in breezy conditions at 11:30am but I went on to ready the plane for take-off.


Here I am installing the GoPro3 camera which would not yet let me read out the First Flight video data it had taken. I hope I can persuade it with some more effort ...

I fueled up the plane with around 15 gallons and opened the doors to get her out.


Then I did a thorough foreflight check.


And here we go, idling and checking the instruments.


Someone here is really focused (and somewhat worried, just slightly).


A last time contemplating what to do if something bad happens, and off we went towards runway 12.



And after another engine run-up (with erratic RPM readings above 5000 rpm), we took off.


I took 25 minutes of circling at 6000 feet MSL to get comfortable, trying stalls and slow flight and could find nothing wrong with the plane. The erratic RPM reading persist above 5000 rpm and it might be a bad connection to the sensor. It is rock solid below 5000, so it definitely working alright. The right wing is ever so slightly heavy and she needs quite some rudder to fly straight. Nothing unexpected though and a nice clean stall at 32 knots with the warning sound coming on at 40 knots. When she stalls the nose drops and that is it. The controls start feeling soft and wobbly at 42 and it worsens with slower speed. One thing I noticed was a high fuel flow warning with the gauge showing 9.9 gallons per hour. I checked the tank and there was no way I was burning fuel at this rate. I switched the electric fuel pump off and the flow immediately went down to 3.8 gals/hr. I am not sure what to make of this but it is an easy fix and I did not lose any fuel.
After those tests and me feeling completely comfortable, I went for a trial approach.






The approach turned out to be a tad high but was definitely land-able so I went for it (easy with a 7000 ft runway). It is amazing though how long the -12 floats when she gets into the ground effect.
And back I went towards the hangar.


Look on the far right if you lost me among all the other planes.


You have to zoom in to see the legendary RV grin or you look at this one after I came to a stop and out of the hot cockpit.


I put the plane away and read out the flight data from the Skyview for later analysis. I've made the logbook entries and went home to celebrate.

To be continued ...

Wednesday, November 27, 2013

Brakes Broken In

Another day of prep work at the hangar. This time, I wanted to break in the brakes with some high speed taxi tests (and the subsequent hard braking). Reliably at 35 knots the nose would come up and I had to focus to not have an accidental First Flight as she really wants to fly now.


I chose a rather cloudy and later pretty breezy day for this activity but at least I learned how to keep her on the taxi way when there are significant cross winds.
Before the wind picked up I was able to complete a WOT static RPM test. As I had pitched the prop to maximum I was expecting to be a bit low on RPMs, it turned out to be stable at 4650. 4800-4900 would be better but this will just affect the maximum speed and I am not concerned about this yet.

Finally I also completed the transponder check at the local FBO and I re-checked the ELT. Everything is a go for a First Flight.

Now lets hope the winds do die down as forecast...

Monday, November 25, 2013

Carbs Balanced

Over the last days I was working on closing up the access covers and reattaching the cowl. It is simply amazing how much time goes just into putting all those screws back in.



I also built a fuel nozzle adapter for the big Mr. Funnel fuel filter.



That way the Mr. Funnel can safely sit on top and hold the fuel while it is filtering through it. This should make fueling a bit easier.

I put the seat backs and the cushions in, for the first time both sets.


All the bottom covers went on and the avionics bay was closed up too.



And the triangle cover for the front of the vertical stabilizer also got attached.


And then today, the carbs were synchronized and the idle adjusted (in reverse order) down to 1400 rpm.

Everything is ticked off the list, except for some high speed taxiing and glazing the brakes and getting my transponder check done. I think I will do this on Wednesday with the First Flight on the following day.

Sunday, November 17, 2013

Static System Tested

The most important thing I had to do today was to complete the static hook-ups on the steam gauges and to test the static system. Having a low leak rate on the static system was the requirement to be able to close up the tail cone and to close up the tunnel.

The sealant on my suction cup system had cured over night and so I was ready to go and connect it.


With the help of a HF vacuum pump (which didn't work well for filling the brake system, because you need a push approach rather than a pull (vacuum) approach), the setup was pretty simple.

The pump itself loses the vacuum fairly quickly which is the reason for putting the shutoff valve in line. The first tests showed a very large leak and the suction cup would not stay on by itself. A bit of blue tape fixed that problem.


The leak was on the back of the altimeter. I had mistaken the nylon plug as a hook-up point for the static line when indeed it was covering a 1/8" NPT threaded hole. I had the right plug to put in and attach the line securely which fixed the leak problem perfectly. Unfortunately, I destroyed my fine German ASI from Winter in the process by forgetting to disconnect the static line from the ASI. Running the altitude up to 8000 ft also increases the airspeed to an astronomical value and the inner mechanics took a permanent hit. I will have to send it in for repair.

The static system had a leak rate of 2:37 minutes to get from 1000 feet AGL to 900. Overall it took 11:22 minutes to get down to 600 feet. The cheap Chinese altimeter has a quite significant leak rate all by itself (tried it by putting the vacuum on the altimeter alone) and it hardly changed when adding the rest of the system so I suppose a pure Dynon system should do much better than this but it is still 2.5 times better than required for the PAP.

While the vacuum tests were running I took care of finalizing the pitot protector.


And fixing some loose cable ties that we found during inspection.


Then I went for the Grande Finale and started the covering of the tunnel by putting the aft bulkhead in.


Isn't it looking nice! The floor panels followed.


At some point I felt like the number of screws was about to match the number of rivets I had put into the plane. But that was nothing compared to the realization that you actually have to pull at least the left wing to get the panel for the flap handle on!
I could not believe it but there was just no way to get the aft part of the cover over the flap handle and under the wing spars otherwise. I actually ended up pulling both wings as one screw did not want to start in the nutplate and I needed a clear view to figure out why.


Eventually I prevailed and the whole assembly came nicely together. However, thinking about taking all this out again in just a year is driving me somewhat insane right now, so I choose not to contemplate this further.
The rest was simple - just a lot of screws still.



I also had my POH reprinted in the latest revision and on card stock to make it a bit sturdier and longer lasting. Considering my luck I'd assume that Van's is going to come out with a new revision by the end of the month.


And concluded a very long work day in the hangar. I am making very good progress though and the next things are:
       - installing the big cover in the seat pan
       - installing the seat backs and cushions
       - installing the lower cowl
       - balancing the carbs
       - installing the top cowl
       - some more taxi tests and engine run up to maximum power

==> First Flight

How would that be for a Thanksgiving?